In this paper, the analysis of an existing calcium chloride evaporation unit was performed to cut primary energy use and emissions. This paper proposes the use of several approaches for retrofit of calcium chloride production. The energy efficiency of the existing process was researched to identify drawbacks and bottlenecks and provide the pathways for process modification. The methodology is based on a systematic analysis and step-by-step reduction of energy use. It uses a Pinch approach, process unit simulation and vapour recompression considering existing process constraints, e.g. product quality, process capacity etc. Two retrofit options of heat exchanger network were proposed with the simulation and design of new equipment. Energy recovery was increased by identification of vapour recompression potential and its appropriate application together with retrofitted exchanger network. All process changes were simulated by commercial software to prove the robustness of proposed energy-saving measures. The case study analyses a chemical plant that exploits the Solvay process and distilled liquid of ammonia production as a feedstock.In the result of retrofit, the energy cost was cut by about 400,000 USD/y and emissions reduction by 18,818 tCO2/y. Steam consumption was reduced by 51% and cooling water decreased by 69%. The economic efficiency of proposed energy-saving measures demonstrates the payback period up to 1.5 years. The roadmap of the step- by-step application of process changes was proposed.